Back to PMW and the unfortunate incident of fitting the wrong head gasket! This meant the mixing of oil and water so that had to be got rid of - see the evidence below as it drained from the sump, looks more like milk than oil doesn't it.
Once that was out of the way then a general clean up and I replaced the oil filter which was contaminated as well of course.
OK, then it was put it all back together and here's a picture of what I sincerely hope is the right gasket fitted the right way up!
From that point I refitted the head and torqued it down, hopefully correctly as I am getting really paranoid now. Once the pushrods were back in I fitted the valve gear and rocker cover before putting in flushing oil. The plan is to run the car for about an hour with flushing oil then drain that, replace the oil filter with another fresh one and refill with new 20/50.
The rest of today's action was refitting the inlet and exhaust manifolds which is much easier to say than do. I actually called it a day about 5PM after struggling with a particularly difficult fixing but it gave in in the end.
Next weekend should see it all back together and an attempt made to get it running again.
No comments:
Post a Comment